**** BEGIN LOGGING AT Sat Dec 01 03:00:01 2018 **** BEGIN LOGGING AT Sat Dec 01 08:39:34 2018 Dec 01 16:05:11 I have downloaded the source for libroboticscape from Jessie 8.7 IoT image (version 0.3.4), and added support for SBUS over the DSM connector. What would be the best way to contribute those changes back into the system? Dec 01 16:06:41 I guess poking RCN might be a good idea, he should be able to point you to the right direction. Or does the packaging state a package maintainer contact? Dec 01 16:08:28 Only Strawsondesign appears to be mentioned in the part I have her. I do not have access to my Beagle right now. Dec 01 16:08:50 jessie is obsolete Dec 01 16:09:34 Yes, but the one we use atm., and the SBUS code is made for it :) Dec 01 16:10:02 RCN is mentioned in debian/changelog, so I'll give him a shout Dec 01 16:11:18 https://github.com/StrawsonDesign/librobotcontrol this is the github repo Dec 01 16:12:03 So James is the contact I guess then Dec 01 16:12:04 but obviously a patch for 0.3.4 is unlikely to be considered useful since that version is ancient and unmaintained Dec 01 16:13:58 Yes. I don't have time to get it into master, but perhaps someone else have Dec 01 16:14:01 all those commits by "Demo User" ... *sigh* -.- Dec 01 22:13:51 hey yall I bought a beaglebone blue a while ago and it was working great up until yesterday when we were working on some things with the gpio pins. The board now does not turn on when plugged in, and only flashes the blue power and on leds briefly when the power button is touched Dec 01 22:14:36 does this mean the power supply is fried? We tested the voltage accross capacitor C34 on the underside of the board and it reads a very low voltage of ~75mV Dec 01 22:15:33 we were playing around with the gpio pins and also accidently unplugged the board from power instead of turning it off properly a few times Dec 02 00:24:00 rip **** ENDING LOGGING AT Sun Dec 02 03:00:01 2018